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Summary of Dangerous Occurrences in Mines (by type)

1 April 2003 to 30 June 2003 (1st Quarter)

Type Date Précis
Collapse Scaffold 26/04/2003 Following the installation of elevated pipe work at a methane utilisation plant on mine surface, a section of tower scaffolding over 5m high was found to have collapsed when contractors returned to the site after the weekend break. No one was injured and no one was working on the scaffold at the time. High winds over the weekend probably blew the unsecured tower over. A proper assessment would have identified this as a foreseeable event and enabled simple preventative measures to be put in place.
Failure of Plant-Shaft 03/04/2003 During coal face salvage operations, a 6 tonne capacity air hoist bottom hook failed at the swivel section. The hoist was part of a complex lift used with a set of 4 tonne manual chain hoists to lift a 7.8 tonne pan set. The failed hook had been connected directly to the rack plate, which induced bending forces. Those involved had been advised of this well-known and understood problem but were all subsequently retrained.
Fall of Ground 03/05/2003 A fall of ground occurred in a fenced off stub roadway in the driven in potash at a large, deep mine. Stub roadways are designed to collapse and provide stress relief on the main access roadways. On this occasion the collapse in the stub roadway extended slightly into the main travelling route and mineral spalled into this roadway. No one was hurt and the mineral, which spalled into the roadway, did not affect ventilation or egress. The maintenance crew leaving the district at the end of their shift discovered the fall. The mine will undertake a weekly review of extraction dimensions, extend the monitoring regime to include confirmation that tell tales are installed and record the readings, and examine the resource allocated to the geotechnical engineer.
Fan Stoppage 01/04/2003 Booster fans were stopped for a period of 40 minutes when a defect occurred on 6,600-volt circuit breaker earth fault protection unit leading to a loss of power to the booster fans. The fans were restarted via the alternative supply. No adverse conditions arose from the stoppage.
Fan Stoppage 01/04/2003 The power to the main fan was lost when a 3,300-volt coupler developed an earth fault. The sensitivity of 11kV and 3.3kV circuit breaker protection was checked pending the commissioning of planned improvements to the electrical distribution.
Fan Stoppage 04/05/2003 During a planned reversal of main ventilation in a substantial section of a large mine, the resultant pressure drop against old workings that had been on the intake side caused emissions of firedamp into the return necessitating the stoppage of two booster fan sites when firedamp levels reached 1.25%. Planned dilution by air slippage at a regulator could not be undertaken as a telephone was inappropriately sited. The maximum firedamp level at one fan site was 1.47%, and at the other levels stayed below 1.25%. The sites were stopped for 59 and 21 minutes respectively, and there were no adverse conditions inbye.
Fan Stoppage 02/06/2003 After a weekend shut down, the main fan at a miscellaneous mine had stopped and failed to restart. All 24 alloy blades of the axial flow fan had broken and detached from the fan shaft. The blades were fitted new and commissioned by the manufacturer two days before the failure. It appears that the main bearing supporting the fan shaft at the inlet end failed allowing the fan shaft to move slightly resulting in the blades catching the inside of the fan cowl. No persons were underground at the time and normal mining work was suspended until normal ventilation arrangements were restored.
Fan Stoppage 15/06/2003 There was an unplanned stoppage of a 3.3kV cluster type underground booster fan when, during planned switching operations, a short circuit flashover developed in a defective live line indicator and resulted in the tripping of the fan's dedicated feeder. The stoppage occurred during a weekend maintenance shift and there was a delay of 60 minutes in restarting the fan. Although ventilation to the mine was reduced by 38% during this period no excessive methane was recorded during the stoppage or subsequent restoration.
Fan Stoppage 22/06/2003 A Booster fan stopped after the temporary loss of power to the mine in a thunderstorm. It could not be restarted for a period of 55 minutes following the failure of the environmental monitoring system leading to the need to put the standby monitoring systems into operation. No adverse conditions arose from the incident.
Fan Stoppage 22/06/2003 During a weekend period, there was a reduction in ventilation to part of a mine when the incoming overhead lines were affected by a series of lightning strikes and severe voltage surges caused widespread trips and extensive loss of surface and underground power supplies. Mine electricians were quickly deployed to restore the supplies to the ventilating fans and the main surface fan was successfully restarted just 23 minutes after tripping. However, re-booting at the surface control room and checks in distribution substations caused a delay of over two hours in restarting the underground booster fans. No one was adversely affected and no excessive methane was recorded.
Fan Stoppage 29/06/2003 On a Sunday morning power was lost to the mine ventilation fans when an 11kv to 3.3kv transformer situated at the bottom of the mine drifts failed. It appears that the secondary winding of one of three individual cores has arced causing a short. The transformer was removed and sent to a specialist workshop for detailed examination and repair.
Fan Stoppage 29/06/2003 At a miscellaneous mine, power to the main fan, which is below ground, was shut off automatically when a resin insulated air cooled 11kV transformer winding developed an inter-turn defect. This was the second such transformer winding to develop such a problem and the transformer will be replaced. The stoppage was prolonged by the need to install a replacement transformer winding, but no adverse conditions arose from the stoppage.
Fire Underground 13/05/2003 A fire broke out in the main return airway of a large colliery as a result of the high-speed mineral conveyor rubbing against belt the structure and hot fibres igniting coal fines underneath the belt. The fire was detected by the environmental monitoring system, investigated by district officials and extinguished using fire hoses. No one was injured, no self-rescuers were used and persons were not withdrawn. Formal enforcement action was taken by serving improvement notices on the mine manager and mine owner.
Fire Underground 21/05/2003 An official responding to a request from the control room operator to investigate a high bearing temperature alarm on a conveyor return end roller found glowing embers on the side plate of the hopper section. The belt was running out of line and rubbing against the side plate generating frictional heat. Only a small amount of material stuck to the side of the plate burned. The conveyor return end was sited below floor level and not cooled by the main ventilation. The response to control room alarms was not wholly adequate and exacerbated the problem.
Fire Underground 27/05/2003 A fire broke out in the engine compartment of a small, diesel powered, tracked dumper working below ground in a mine where ground stabilisation work was being undertaken. The driver put out the fire with a portable 6kg dry powder extinguisher after the operation of the on-board Fire Suppression System (fire suppression system), failed to quell the fire completely. No persons were injured, no self-rescuers were worn, and equipment damage was minimal. Hydraulic mineral oil, leaking from a damaged hydraulic hose, was the fuel and the hot engine exhaust the most likely source of ignition. Preventative measures include, properly designing an on-board fire suppression system for the vehicle in question and others at the mine, re-routing and shrouding of hydraulic hoses and electric cables and fitting a portable fire extinguisher to each vehicle.
Fire Underground 30/05/2003 An official and two workmen travelling outbye at the end of the night shift smelled burning. They traced the source to a trunk conveyor receiving hopper where the blind side bearing on the idler controlling the belt through the plough had collapsed causing the belt to rub against the hopper, generating heat and igniting coal fines. They put out the fire with water and cleaned up to ensure no residual burning material remained. The fire was not detected by the environmental monitoring. The idler has since been replaced with one equipped with higher duty bearings and a review of the suitability of bearings constructed with plastic cages has been carried out.
Fire Underground 02/06/2003 During an engine fluids level check, initiated loss of power, a fire broke out below ground in the diesel engine compartment of a telehandler when pressurised transmission fluid leaked from a dipstick hole and dripped onto the adjacent hot exhaust. The mine subsequently found that the transmission breather was blocked. The on-board automatic fire suppression system relied on a contrived arrangement to hold the firing handle open, but this was missing. The on-board manual fire suppression system operated but the simple 2 nozzle system failed to quell the fire completely. The fire was easily extinguished with the vehicle's portable extinguisher and no person suffered any ill effects.
Fire Underground 18/06/2003 A shift charge mechanical engineer detected a strong burning smell whilst examining a site for a conveyor repositioning. He found a heating on the blind side of the receiving conveyor adjacent to the plough bottom idler. He summoned some nearby conveyor maintenance workers who cleared away some accumulated coal spillage and sprayed the area with water. There was no defect on the idler and the bearings were intact. The fire was not detected by the environmental monitoring. Records indicated that the ventilation quantity was 17.34m3/s.
Fire Underground 21/06/2003 An FSV driver below ground smelled burning and tracked it down to a sparking 298kW 6.6k V conveyor drive motor. He stopped the conveyor and saw flames around the motor drive shaft. He quickly extinguished the fire with a single portable dry power extinguisher. No person suffered any ill effect, or wore a self a self-rescuer, or was withdrawn. Heat from the catastrophic failure of the roller cage in the motor drive end bearing had caused leakage and ignition of bearing grease. Bearing temperature monitoring and in-service vibration detection are to be improved.
Fire Underground 25/06/2003 A fire occurred in an in seam intake conveyor roadway when a bearing at one end of non-driven return end sprocket of metering chain conveyor failed and generated heat. Workers in a heading several hundred metres inbye smelled smoke, went to investigate and saw 0.5m high flames above the sprocket bearing. They stopped the panzer and flames went out but they applied a dry powder extinguisher and cooled area with water. No one was withdrawn and no one wore self rescuers. The bearing failed due to ingress of fine coal through the seals, which were probably damaged due to misalignment of the sprocket. A temperature-monitoring device had given warning previously but the investigating fitter tensioned the panzer thinking over-tension to be the cause. He did not check bearing thoroughly and appears to have inadvertently detached temperature probe from bearing during operation. Improvements to design, maintenance and response of craftsmen to temp warnings are being pursued to prevent a recurrence.
Ignition of Gas Underground 25/06/2003 In the underground repair workshop of a large miscellaneous mine, a fitter working on a diesel-powered telehandler sustained minor burns when the vehicle's 95Ahr 12V lead-acid battery exploded violently. Hydrogen gas emitting from the battery was ignited by a spark from the fitter's angle grinder and the flame flashed-back into the top of the battery. Batteries will in future be removed or shielded if there is a likelihood of sparks falling on or near them.
Locomotives 01/04/2003 Two wheels of the leading cab of a 50 hp Bo-Bo locomotive derailed when the locomotive was driven into a passbye and made contact with a pipe joint on a methane drainage range. The track and clearances had been commissioned during December 2002 and at that time only one methane range was in the roadway. A second range, which the locomotive struck, was installed directly beneath the first range during January. The mine is to pursue an improved procedure for identifying and evaluating changes that might have an adverse effect on clearances in transport roads and to feed that into the design.
Locomotives 22/04/2003 A steel tyred battery powered locomotive travelling at slow speed hauling a material load was brought to rest by derailment whilst travelling round a 20m radius turnout curve. Floor movement had resulted in excessive track twist, which was being checked regularly by observing the passage of a loco and reporting any outer wheel lift. However, the locomotive had just had new wheel sets fitted, which reduced the margin against derailment. The turnout was re-laid immediately after the incident. Track twist should be properly measured against prescribed standards, and where necessary fitted with a checkrail.
Locomotives 29/04/2003 While turning round a 150hp double-ended, Bo-Bo locomotive at a passbye at an inbye main manriding terminus, all four wheels of the leading bogie detailed at slow speed just beyond the points. No one was injured and no serious damage resulted. The points blades were split and out of adjustment and the locking fish tail for the LH blade had come out of its locating saddle, which had been displaced. Once the points were readjusted and bolts tightened the worked satisfactorily. Tests showed that when the locomotive wheels just clear of the points the operator could see the nearside blade but could not see the offside blade sufficiently well to ensure that it was correctly set. It is likely the maladjustment was caused by the derailment and that the most likely cause of the incident is that the loco wheels were too close to the points preventing the LH rail fully closing and the operator from seeing this.
Overturn Dangerous Substance 04/06/2003 On the surface of a tourist mine during major construction works, a 13 tonne tracked hydraulic excavator overturned. The unwitnessed incident occurred when the excavator was negotiating a short but steep incline slope between working levels. The machine tilted backwards onto its counterweight and landed upside down. The driver who was apparently wearing a lap belt escaped injury. There were deficiencies in operator competency, an absence of suitable information regarding the safe use of excavators on steep slopes and inadequate ground works design by the mine owner and principal contractor.